| Airport Safety • AW&ST • Barbour Air Safety • Joe Chase • de Florez Flight Safety • Brownlow Publication • Crane Founder’s |
| AeroSafety World • Accident Prevention • Airport Operations • Aviation Mechanics Bulletin • Cabin Crew Safety |
| Membership Categories • Member List • Corporate Application • Individual Application • Endowment Fund |
| International Air Safety Seminar • European Aviation Safety Seminar • Corporate Aviation Safety Seminar • Future Seminars |
| Flight Safety Digest • Helicopter Safety • Human Factors & Aviation Medicine • Guidelines for Authors |
| News Releases 2008 • News Releases 2007 • News Releases 2006 • News Release Archive 1995–2005 • Photo Gallery |
| Meritorious Service • Heroism • President’s Citation • Professionalism • Bendix Trophy • Human Factors • Lifetime Achievement |
|
|
These publications are in Acrobat® Portable Document Format (PDF) and require a copy of Adobe Reader®. If you do not have a copy of Adobe Reader, you can download and install a free copy from http://www.adobe.com/products/acrobat/readstep2_allversions.html. November–December 2002Aerial Ambulance Loses Engine Power During Approach in Dense Fog 6 pages. [PDF 80K] After diverting a flight because of low fuel, the pilot was told that visibility was approximately five meters (16 feet) at the highway intersection where he attempted to land a Bell LongRanger III. The engine stopped producing power during the approach, and the helicopter struck terrain. September–October 2002Abrupt Maneuver and Mast Bumping Cited in Loss-of-control Accident 4 pages. [PDF 42K] Witnesses said that the Fairchild Hiller FH-1100 helicopter was being flown at low altitude when the main rotor separated and a rotor blade struck the cabin. July–August 2002Data Show 50 U.S.-registered Helicopters Involved In Wire-strike Accidents From 1996 Through 2000 6 pages. [PDF 83K] In each of the accidents, the helicopter was either destroyed or damaged substantially. Fifteen accidents resulted in at least one fatality; nine other accidents resulted in serious injuries. May–June 2002Unsecured Fasteners in Tail-rotor System Faulted for Bell UH-1H Loss of Control 6 pages. [PDF 154K] New Zealand investigators said that the failure to install split pins during maintenance likely caused nuts and bolts in a tail-rotor-blade pitch-control mechanism to become loose, leading to the pilot’s loss of control of the ex-military helicopter during approach and landing. March–April 2002Boost Pump Failure Starves Bell 214B Engine of Fuel 6 pages. [PDF 119K] Canadian investigators said that the aircraft flight manual did not adequately describe the potential consequences of a boost pump failure and that the pilot’s lack of recurrent training might have affected his ability to conduct an autorotation. January–February 2002Sikorsky S-76B Strikes Water During Approach to North Sea Oil and Natural Gas Production Platform 8 pages. [PDF 44K] The flight crew was conducting a go-around in dark-night conditions and did not observe the high rate of descent that followed a large power reduction during the turn to final approach. The crew’s application of collective to reduce the sink rate came too late to prevent the helicopter from striking the water. |
|||||||||||||||||||||
| Copyright ©2001–2008. All Rights Reserved. Flight Safety Foundation 601 Madison Street, Suite 300 • Alexandria, Virginia U.S. 22314-1756 Telephone: +1 (703) 739-6700 • Fax: +1 (703) 739-6708 Privacy Statement |